202102

增设0号高压加热器的汽源优化和控制策略研究
发布人:网站管理员 发布时间:2021/3/9 点击次数:135次
  

增设0号高压加热器的汽源优化和控制策略研究
石卫兵1,周刚2,3,刘桂生1,王煜伟1,林琳2,3,王勇2,3
(1. 国电江苏谏壁发电有限公司,江苏 镇江 212006;2. 西安西热节能技术有限公司,陕西 西安 710054;3. 西安热工研究院有
限公司,陕西 西安 710054)
摘要: 以一330 MW 机组增设0 号高压加热器为例,研究了高加汽源整体优化问题,分析了投运0 号高压加热器后机
组能耗和环保指标的变化情况,并通过对控制策略的合理优化,使0 号高压加热器可随着机组负荷变化自动调节抽汽量
并切换为热备用状态。研究结果表明,汽源优化后,汽轮机热耗率比优化前下降了12.4 kJ/(kW·h)。
关键词: 0 号高压加热器;汽源优化;热耗率
中图分类号: TK269+.6     文献标识码: A     文章编号: 2095-0802-(2021)02-0157-03
Study on Steam Source Optimization and Control Strategy of Adding No.0 High Pressure Heater
SHI Weibing1, ZHOU Gang2,3, LIU Guisheng1, WANG Yuwei1, LIN Lin2,3, WANG Yong2,3
(1. Guodian Jiangsu Jianbi Power Generation Co., Ltd., Zhenjiang 212006, Jiangsu, China; 2. Xi'an TPRI Energy Conservation
Technology Co., Ltd., Xi'an 710054, Shaanxi, China; 3. Xi'an Thermal Power Research Institute Co., Ltd., Xi'an 710054,
Shaanxi, China)
Abstract: Taking a 330MW unit with No.0 high pressure heater as an example, this paper studied the overall optimization of high
steam supply, analyzed the changes in energy consumption and environmental protection indicators of the unit after the operation
of No.0 high pressure heater. Through the reasonable optimization of control strategy, the steam extraction of No.0 high pressure
heater was automatically adjusted with the unit load change and switched to the hot standby state. The research results showed
that after the steam source was optimized, the heat consumption rate of the steam turbine reduced by 12.4 kJ/(kW·h) than before.

Key words: No.0 high pressure heater; steam source optimization; heat consumption rate